In my first posting, I said that one of my ongoing projects was finishing the elevation rotator (EL rotator) that is part of my amateur satellite setup. Well, it's still not finished, but at least it is back in action after damage (accidentally caused by me) had stopped it elevating for several weeks :-)
I am going to write an article about the design and construction of the EL rotator that, I hope, will be published in Oscar News. I’ll also put the information on my website. But, in brief:
- A satellite TV linear actuator rotates the antenna boom in the vertical plane.
- A potentiometer, housed in a metal box and connected to the boom by a pantograph arrangement, senses the amount of elevation.
- The ARS hardware and software (from EA4TX) in my shack measure the elevation and commands the linear actuator up or down as required.

- Calibrating it more precisely than I had when first getting it going.
- Trying to cure RF interference coming from the actuator motor when it is in motion (noticeable and annoying but not a showstopper).
- Completing the waterproofing by putting some sealant around the lid of the metal box in which the position-sensing potentiometer is housed.
With hindsight, a number of options were available for fixing it:
- Replacing the potentiometer.
- Rotating the potentiometer so that an undamaged portion of the track is used to measure the 90 degree swing of the elevator.
- Using PCB cleaning spray to flood the carbon track in the potentiometer to see if this cleared whatever was causing the problem.
- Blowing a strong jet of air from an aerosol into the body of the potentiometer to achieve the same thing.
However, when I started the repair, I discovered that I could not shift the grub screws, due to a combination of corrosion and the Loctite applied to them when installed. In fact, I stripped the slots on the screw heads trying to free them.

- Drastic surgery (using a grinding wheel on a Dremel) to separate the potentiometer assembly from the pantograph arm.
- Soldering a new socket onto the pantograph arm.
- Cutting and fitting a new shaft extension for the potentiometer.
- Fitting the new potentiometer itself.
This all took time but went pretty smoothly. I waterproofed the grub screws (using self-amalgamating and PVC tape) to avoid a repeat of that problem. And I have not used sealant on the metal box, relying instead on what is a fairly snug mechanical joint. I still have to sort out the other two jobs (final calibration and dealing with the RFI), but at least I am back in action.
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